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R&D (Roberts Linkage)
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KoheiMitsuhashi - 01:14, Friday 01 September 2023 (3317)Get code to link to this report
Fitting IP's resonant frequency

What I did:
I fited the resuts of IP's resonant frequency to theoretical value.


The equation used for fitting was atttached.
f is IP's resonant frequency.
k_e is spring constant of IP's flex joint .
k is s anti spring constant.
g is gravity constant.
l is length of IP.
m_0 is mass of IP.
M is weight on IP.

From fitting, m_0 is 1.08 kg, k_e is 131 N/m, l is 2.48 m.
 

The results and fitting picture was as follows.
X-axis is weight on IP top, y-axis is IP's resonant frequency.

Images attached to this report
3317_20230831175947_texclip20230901005920.png 3317_20230831180026_fittingofipsresonatfrequency.png
R&D (Roberts Linkage)
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KoheiMitsuhashi - 00:34, Wednesday 30 August 2023 (3316)Get code to link to this report
diagonalization of IP's matrix

What we did:
We diagonalized the matrix of IP, and checked how much diagonalization was.

The matrix's values form LVDTs to imaginally L-axis and T-axis were as follows.

  L T
H1 +0.20 -0.04
H2 -0.07 -0.12
H3 -0.09 +0.13

The matrix's vakues from L-axis and T-axis to actuators were as follows.

  A1 A2 A3
L -2.20 +2.45 +0.46
T +0.45 +3.21 -2.71

I measured the trasfer function from L,T to L,T respectively.
The pictures was attached.
I concluded it was good at some extend.
 

Images attached to this report
3316_20230829173324_30011206871.png 3316_20230829173332_30011206872.png 3316_20230829173337_30011206873.png 3316_20230829173343_30011206874.png 3316_20230829173349_30011206875.png 3316_20230829173355_30011206876.png 3316_20230829173750_30011206877.png
KAGRA MIR (Polarization)
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MarcEisenmann - 09:33, Thursday 24 August 2023 (3314)Get code to link to this report
Comment to spare ETMY measurement started (Click here to view original report: 3311)

The measurement seems to go fine and is mostly finished.

However, because of the new failure of air conditioning the temperature and humidity increased quite a lot in TAMA.

It's about 30deg in main building and quite more inside clean room.

just for safety I turned off PCI laser.

R&D (Roberts Linkage)
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KoheiMitsuhashi - 21:12, Sunday 20 August 2023 (3312)Get code to link to this report
Summary of Roberts' Linkage tabletop experiment.

Mitushahshi

I summarized the tabletop experiments of Roberts' Linkage.

What I did
The followings are what I did.

  • I measured the resonant frequency of Roberts' Linkage with changing COM.
  • I checked the difference of resonant frequencys between x-axis and y-axis(The definitions of these axes are written on below sentence).

Set up
I attached the picture(Fig1).
The Roberts' Linkage was shaked by coil magnet actuator powered by FFT analyzer.
The displacement of it's was detected by photo sensor.
I measured the transfer function from coil magnet actuator voltage to photo sensor read out voltage.

Measurement results
Firstly I mentioned resonat frequency and COM position. I attached the picture(Fig2).
The results says that the resonant frequency get lower and lower when Roberts' Linkage was tuned at hight COM points.
The gap are there between first mesurement and second measuremt. I thought the reasons are some coupling by different tension on wires and by human error with tuning COM(this is most properly).

Secondary, I mentioned the strange peak. I attached the power spectra density plot.
The peak at 71mHz is the resonant, and harmonic of it also are there(rabeled blue).
On the other hands, the strange peak that it is not reasonable by above mention also are there(label green). 
The paper "F. Garoi et al., Passive vibration isolation using a Roberts Linkage, Rev Sci Instrum 74, 3487-3491(2003)" reported that there are cross coupling.
So I measured the x-axis and y-axis resonat frequency. The definition of x-axis is following on the road of 20m interference site(Fig3).
I attached the results. The red one is x-axis, and the blue one is y-axis.
I realized that these axes have a difference resonat frequencys, and conclued that the strange peak is from y-axis' resonant frequency (cross coupling).

Images attached to this report
3312_20230820134736_fig1.png 3312_20230820134829_2.png 3312_20230820134927_3.png 3312_20230820135004_4.png 3312_20230820135048_5.png 3312_20230820135116_6.png
KAGRA MIR (Polarization)
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MarcEisenmann - 16:37, Thursday 10 August 2023 (3311)Get code to link to this report
spare ETMY measurement started

[Aso, Marc, Michael, Rishabh]

We installed spare ETMY with ears up (ie reversed top/down with respect to KAGRA installation) on the translation stage.

It helped a lot to remove the front top right metal support looking from the laser side for the installation.

After small realignment of the 2 photodetectors I checked the mirror center by trying to find the position where the signals drop to 0 (ie edge of the mirror).

X_center = 393.5 mm and Y_center = 155.5 mm.

Then I started measurement with Spol at the input (HWP = 351.2 deg) with maximum AC and DC dynamic range (1V) to take map over 70 mm radius with 1 mm step.

I'll keep these settings during holydays to avoid saturation.

Comments related to this report
MarcEisenmann - 09:33, Thursday 24 August 2023 (3314)

The measurement seems to go fine and is mostly finished.

However, because of the new failure of air conditioning the temperature and humidity increased quite a lot in TAMA.

It's about 30deg in main building and quite more inside clean room.

just for safety I turned off PCI laser.

KAGRA MIR (Polarization)
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MarcEisenmann - 00:25, Wednesday 09 August 2023 (3310)Get code to link to this report
birefringence measurement preparation

I realigned the beam at normal incidence using the razor blades using input power of 1.59mW.

After realignment, I got angle of incidences of 0.009 deg and 0.0059 deg for vertical and horizontal direction respectively.

I tuned the input HWP and QWP to have input s polarized light by minimizing the p polarization component.

With current configuration, 'DC' corresponds to S pol and 'AC' to P pol.

I took 10mn of data with each polarization to finalized the setup calibration.

I was planning to measure the ILM sample birefringence but could not find suitable holder (30mm diameter ; 15 mm thickness).

We plan to start instead with spare ETMY measurement.

Birefringence mitigation (General)
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MarcEisenmann - 00:21, Wednesday 09 August 2023 (3309)Get code to link to this report
HWP birefringence measurement

I reinstalled the output cross-polarizer and also installed a HWP (WPQ-10640-2M from SigmaKoki) just after LC2.

I am now scanning the LCs voltages with various step to measure birefringence in 'electronic Soleil-Babinet' mode.

Birefringence mitigation (General)
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MarcEisenmann - 10:50, Monday 07 August 2023 (3308)Get code to link to this report
long measurement

The measurement started in elog 3295 finished.

It consists of about 6.3 millions couples of votlages applied to LC1 and LC2.

Figures 1 to 3 reports the resulting polarization states which is similar to previous measurement despite the 90 deg rotation of LC1.

Somehow we have an overall phase difference of 90 deg as before. I'll cross-check simulations.

When measurement finished, the LCs temperature was about 31degC. This indicates a stronge heating as the usual LC temperature is about 24 degC before heating for temperature control.

This seems to be related to the air conditioning failing noticed by Takahashi-san that could also explain the strange power fluctuations of the FDS laser reported in elogs 3306 and 3307.

Images attached to this report
3308_20230807034010_polarotfull.png 3308_20230807034015_polaretarfull.png 3308_20230807034019_polagenfull.png 3308_20230807034736_rotatinghwpgen.png 3308_20230807034740_rotatinghwpretar.png 3308_20230807034743_rotatinghwprota.png
R&D (FilterCavity)
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ChienMingWu - 02:05, Wednesday 02 August 2023 (3307)Get code to link to this report
Measured FIS of 5.4 dB at 25mW and 5.7dB at 40mW green power

8/1 [Chien-Ming and Hsun-Chung]

We measured around 5.4dB squeezing and 11.4dB antisqueezing at 25mW green pumped,
                             and 5.7dB squeezing and 16.7dB antisqueezing at 40mW green pumped.

Without green pump, OPO T=7.107 kOhm; BAB=192mV, p-pol PLL: 225MHz
At 25mW pump, OPO T=7.118 kOhm; BAB max=1.27V, min=80mV, p-pol PLL:165MHz
Nonlinear gain=6.61

At 40mW pump, OPO T=7.120 kOhm; 
BAB max=3.28V, min=40mV, p-pol PLL:130MHz
Nonlinear gain=17.08

The SHG power in front of MZ drops to
151.5mW today.
In addition, we found the LO power to HOM also drops to 1.68mW. We can't increase it by alignment, so we have to replace the 
OD0.3 ND filter before IRMC to OD0.1.
As a result, the LO power is restored to 1.94mW.
We suspect that the output power of the main laser may be continuously decaying, causing the SHG and LO power to drop!


Attached are two squeezing measurement at different pump powers. It is worth mentioning that when the HOM DC cable is too close to the oscilloscope, some noise peaks will appear obviously, especially on dark noise.
The units setting parameters of SR785 was also attached.

Images attached to this report
3307_20230801185323_230801sq25mw.png 3307_20230801185342_230801sq40mw.png 3307_20230801185521_sr785unitssetting.jpg
R&D (FilterCavity)
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ChienMingWu - 00:51, Wednesday 02 August 2023 (3306)Get code to link to this report
OPO temperature is not optimized resulting in poor squeezing measurement

7/31 [Chien-Ming and Hsun-Chung]

We investigate the reasons for the squeezing level decline on 28th July http://www2.nao.ac.jp/~gw-elog/osl/?r=3305.
Originally we suspected it was caused by poor cleaning of the optics, but today we found out that the phase-matching temperature of OPO is not at the optimal value.

On 7/28 we set OPO T=7.159 kOhm with 25mW green pump and T=7.184 kOhm with 40mW green respectively in order to lock the p-pol at 270MHz.
Today we check that the optimal value of OPO T should be set near 7.107 kOhm to achieve the maximum nonlinear gain.


OPOT=7.107k; 25mW green; BAB Max=1.26V; p-pol=33MHz*5=165MHz.
Without green; BAB=196mV-6mV(Background)=190mV; p-pol=49MHz*5=245MHz.
Therefore the nonlinear gain=6.63 at 25mW pump.

HOM visibility:
LO at AMC: TEM00=5.96v; hom=2.4mV+2.4mV; mode-matching: 99.92%
BAB at AMC: TEM00= 196mV; hom=6.4mV+1.8mV; mode-matching: 95.98%

SHG output power in front of MZ drops to 165.5mW even if the SHG temperature and alignment are optimized (194.9mW on 7/28)

We preset the SR785, however, the parameters are incorrect so the squeezing measurement is weird today.

R&D (FilterCavity)
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ChienMingWu - 00:04, Sunday 30 July 2023 (3305)Get code to link to this report
Measure FIS at 25mW and 40mW after clean some optics
7/28 [Chien-Ming and Hsun-Chung]
At first, the SHG is 119.7mW in front of MZ.
We correct the HOM DC balanced from -10mV to 0mV by fine-tuning HOM BS Yaw.

Hsun-Chung bought some glass dropper bottles to hold acetone (buy from HANDS).
We cleaned some optics on the optical path of HOM and SQ and then checked the BAB alignment at AMC.
TEM00=206mV; hom=5.6mV+5.6mV; mode-matching:94.8%

In the beginning, the OPO T was 7.117k(p-pol is 270MHz) with pump 25mW, the BAB max=52mV, min=24mV.
After setting the OPO T to 7.159k(p-pol is 270MHz), the BAB max= 952mV, min= 104mV
At the 25mW green pump, we measured 4.47dB squeezing and 8.43dB anti-squeezing which is worse than yesterday's result.
Therefore, those optics may not be cleaned well.

Then we measured twice FIS at the 40mW pump, got 5.28dB SQ and 12.13dB Anti-SQ at first, and 5.29dB SQ and 11.65dB ASQ at second.
Before the second measurement, the MZ failed to lock again. The reason is that the output power of the SHG seems insufficient (100mW in front of MZ).
By setting the temperature of SHG from 3.158k to 3.123k, the green light in front of MZ becomes 194.9mW.
The BAB max=1.54V and min=152mV at 40mW pump and OPO T= 7.182k (p-pol is 270MHz).
Without green pump, the BAB=234mV at OPO T=7.121k (p-pol is still 270MHz)
Therefore, the nonlinear gain is 6.58 at the 40mW pump.

The attachment is the comparison of the measurement data for two days
Images attached to this report
3305_20230729170141_727vs728fis.png
R&D (FilterCavity)
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ChienMingWu - 01:59, Friday 28 July 2023 (3301)Get code to link to this report
FIS 5 dB squeezing measured

7/27 [Chien-Ming, Hsun-Chung]

Summary:

 We measured about 5 dB squeezing and 11 dB anti-squeezing at 25.1mW pump power.

 

 Current parameter settings:

DDS1 ch1 SHG & IRMC demod. phase 140 deg.
DDS2 ch2 GRMC demod. phase 200 deg.
DDS3 ch3 P-Pol PLL 54MHz (0 mW green)
38MHz (25 mW green)
DDS3 ch1 homodyne phase SQ: 75 deg
ASQ:140 deg

Details:

ch1
ch1

CC light is not coupled into the OPO at all, after realignment

CC: TEM00=19.8mV; hom= 4.6mV+2.2mV; mode-matching: 74.4%.

 

SHG output power dropped to half, so we realign the incident 1064nm again, and now the green power before MZ is 126.7mW.

When the green light is well coupled into OPO, the GRMC and MZ are not easy to be locked. Seems to be interference from the feedback light.

 

When put the LO flip mirror back, the LO light is not coupled into the 2nd HOM PD at all.(but it worked yesterday)

We have to adjust the lens position to achieve HOM DC balance.

 

 

The BAB nonlinear gain today without green and with 25.1mW green again: (this time we have considered the background by blocking the BAB.)

without green, Max=240mV-6mV(BG)= 234mV ; OPO T:7.117
with 25.1mW green, Max=1390mV (Min=96mV) ;OPO T:7.119

SQ: 75 deg
ASQ:140 deg
Pump power (mW) 0mW 25.1mW
OPO temperature (kOhm) 7.117 7.119
P-Pol PLL frequency (MHz) 270 190
BAB maximum (mV) 234 1390
nonlinear gain 1 5.94
SQ: 75 deg
ASQ:140 deg


cc1 cc2 can be locked smoothly.

cc1 error signal EPS1OUT Vpp=266mV.

cc2 error signal EPS1OUT drifts up and down over time in the range of 348mV, the Vpp is around 170mV.


The parameters we use for SR785 are:

128Hz~102.4kHz AC 
FFT1 LogMag Hanning

Compute Avgs: Yes; type: Exp./cont; # Avgs: 100 ; Display Avg: RMS
SAVE: Display to Disk

SQ: 75 deg
ASQ:140 deg
SQ: 75 deg
ASQ:140 degS
Images attached to this report
3301_20230828113103_230727sq25mw.jpg
R&D (FilterCavity)
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ChienMingWu - 23:16, Wednesday 26 July 2023 (3297)Get code to link to this report
realigned green to OPO, measured nonlinear gain, and HOM visibility

[Chien-Ming, Hsun-Chung]

 

To check the alignment of green pump to OPO, we measure the nonlinear gain of BAB maximum in 1st HOM PD.

without green, Max=248mV (forgot to subtract the background); p-pol PLL 270MHz; OPO T:7.127

with 25.1mW green, Max=1540mV (Min=120mV) (also forgot to subtract the background) ; p-pol PLL 190MHz; OPO T:7.129

after two hours..

with 25.1mW green, Max=1200mV (Min=120mV) ;OPO T:7.129

I realign the green to OPO and adjust temp. of OPO

with 25.1mW green, Max=1580mV (Min=120mV) ;OPO T:7.123

without green, Max=248mV; OPO T:7.122
 

green power (mW) 0mW 25.1mW
OPO temperature (kOhm) 7.122 7.123
p pol PLL frequency (MHz) 270 190
BAB maximum (mV) 248* 1580*
nonlinear gain 1 6.37

*This value does not check and subtract the background caused by p-pol.

 

To optimize HOM visibility, we realign the OPO output BAB mode matching at AMC.

Before: TEM00=164mV; hom=34mV+8mV+8mV ; 76.6% mode-matching

After: TEM00=218mV; hom=8mV+8mV ; 93.2% mode-matching

 

Realign the IRMC mode matching by monitoring the T of IRMC servo
Before: TEM00=920mV; hom=48mV+48mV; 90.6% mode-matching

After: TEM00=960mV; hom=56mV; 94.5% mode-matching

 

IRMC PDH signal and SHG PDH signal are using the same DDS channel to demodulate, so readjust the DDS phase from 110 to 140 degrees to reach a compromise. (Used 160 degrees to reach the best SHG PDH signal yesterday)

 

LO mode matching at AMC

TEM00=6.64V; hom=16mV ; 99.76% mode-matching

 

GRMC failed to lock again, checking the PDH signal and reloading the DDS2 to change the phase of GRMC demod. from 165 degrees to 200 degrees (Used 100 degrees yesterday).

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ChienMingWu - 09:29, Wednesday 26 July 2023 (3296)Get code to link to this report
realigned BAB, p-pol, SHG, GRMC,and MZ

7/25

[Chien-Ming, Hsun-Chung, Marc, Michael]


We realign the P-pol and BAB by using the steering mirrors before PBS

p-pol :

Before: TEM00=1.78V; hom=460mV+100mV ; 76% mode-matching
After: TEM00=1.92V; hom=160mV+160mV ; 85.7% mode-matching

 

BAB :
Before:  TEM00=1.05V; hom=264mV+200mV+180mV+140mV+50mV=834mV ; 55.7% mode-matching

After:  TEM00=1.17V; hom=232mV+200mV+200mV+140mV+50mV=822mV ; 58.7% mode-matching


To check the green pump to OPO alignment, we use BAB to optimize the nonlinear gain.
Without green, we phase lock the p-pol at 270MHz and tune the OPO temp. from 7.147 to 7.123.

we obtain the maximum BAB output by putting the power meter before homodyne BS.

The value is 1.78V - 900mV(background) =  880mV (however, power meter is set at 532nm)

 

When we want to introduce the green pump, we failed to lock GRMC and MZ, also the SHG output is not good.

 

So I realign the SHG input 1064nm beam,
Before:TEM00=1.58V; hom=1.28V; 55.2% mode-matching
After:TEM00= 354mV; hom:10mV; 97.3% 
mode-matching

 

Then I check the PDH signal of SHG and optimize it by changing the phase from 110 degrees to 160 degrees.

I successfully locked SHG. The power in front of MZ is 132.6 mW.

 

Then I check the PDH signal of GRMC, it's quite small, the S/N=280mV/50mV ~ 280mV/100mV.

Optimizing this signal by adjusting the mirror at the GRMC input reflected beam and then reloading the DDS2 to change the phase of GRMC demod. from 165 degrees to 100 degrees. We obtain the S/N= 126mV/15mV.

Finally, we successfully locked GRMC after adjusting the parameters of the servo.

After locking the MZ, the pump power corresponding to the MZ offset is as follows:

 

MZ offset vs green pump power
MZ offset Green pump power
4.0 15.7 mW
4.1 21.6 mW
4.2 27.0 mW
4.3 32.3 mW
4.4 37.8 mW
4.5 43.4 mW
4.6 49.0 mW
4.7 54.6 mW
4.8 59.6 mW
4.9 64.9 mW
5.0 70.1 mW
Birefringence mitigation (General)
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MarcEisenmann - 19:04, Monday 24 July 2023 (3295)Get code to link to this report
larger polarization states generation

I scanned LC1 and LC2 voltages from 0 to 25V with 0.02V step at 30degC.

Today I rotated LC1 by +90 deg to investigate the phase difference with respect to simulation.

I started measurement between 0 to 25V with 0.01V step at 30degC.

Images attached to this report
3295_20230724120354_polarot5.png 3295_20230724120402_polaretar5.png 3295_20230724120407_polagen5.png
Birefringence mitigation (General)
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MarcEisenmann - 20:15, Thursday 20 July 2023 (3293)Get code to link to this report
polarization states generation with smaller step

I tried to generate again polarization states but this time with 0.01V increment instead of the previously used 0.05V.

Because of TAMA visit I had to turn off the laser before the several days long measurement finished.

In any case, the results shows again good agreement with previous results and simulation and also higher polarization states coverage.

Images attached to this report
3293_20230720131540_polarot4.png 3293_20230720131545_polaretar4.png 3293_20230720131550_polagen4.png
Birefringence mitigation (General)
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MarcEisenmann - 20:11, Thursday 20 July 2023 (3292)Get code to link to this report
Comment to arbitrary polarization states generation (Click here to view original report: 3290)

This result can be compared with simulation were I assumed for now same retardance vs voltage and extinction ratio equals to 1.

The rotation and retardation are shown in figures 1 and 2.

The retardation agrees really well with measurement if we wrap the measured retardation to positive values (fig 3).

Forthe rotation, it seems we have some kind of 90deg offset. I'm wondering if it could be because the first LC is rotated by -45deg instead of +45deg.

Images attached to this comment
3292_20230720131057_polarotsimu.png 3292_20230720131102_polaretarsimu.png 3292_20230720131219_polaretar3wrapped.png
R&D (FilterCavity)
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MarcEisenmann - 20:07, Thursday 20 July 2023 (3291)Get code to link to this report
realigned MZ and GRMC

[Chien-Ming, Hsun-Chung, Marc, Michael]

First we found out that the power just after SHG is a bit lower than usual (measured 216mW) so we might have to tune its temperature.

Then, we found that MZ and GRMC were quite misaligned (especially in pitch).

We placed a power meter in transmission of GRMC to realign them.

First, the power had some periodic increase so we reduced the MZ scan period from 10 to 0.

Also, realigning it helped. After realignment we got :

1st arm TEM00 2.54V ; hom = 0.18V : 93% mode-matching

2nd arm TEM00 308mV ; 3 hom each = 6.4mV  ; 94%

We tried to lock GRMC and MZ but the lock was not stable. So we had to increase the gains as follow:

increased GRMC gain to 3.1 from 1 ; increased MZ gain from 1 to 3

Finally, they locked and with MZ offset 4.54 we measured 44.7mW in transmission of GRMC in good agreement with the expected value.

Birefringence mitigation (General)
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MarcEisenmann - 10:20, Wednesday 19 July 2023 (3290)Get code to link to this report
arbitrary polarization states generation

After spending a lot of time generating polarization states and rotating the output polarizers I found out that this method is not too precise.

While the overall shape is similar to simulation, there are several points were the fitting is failing and gives polarization rotation 0 or 90 deg and retardation 45deg.

This is especially annoying as the measurement is far longer than expected (poor vi implementation limited measurement speed to 6Hz and need to rotate at least 36 times the ouput polarizer)...

In the end I removed the ouput polarizer and used the polarization camera readout.

THe measurement are agreeing now really well with simulations.

Note that in the simulation an arccos of the retardation limits the retardation to positive values only.

Images attached to this report
3290_20230719031918_polarot3.png 3290_20230719031923_polaretar3.png 3290_20230719031927_polagen3.png
Comments related to this report
MarcEisenmann - 20:11, Thursday 20 July 2023 (3292)

This result can be compared with simulation were I assumed for now same retardance vs voltage and extinction ratio equals to 1.

The rotation and retardation are shown in figures 1 and 2.

The retardation agrees really well with measurement if we wrap the measured retardation to positive values (fig 3).

Forthe rotation, it seems we have some kind of 90deg offset. I'm wondering if it could be because the first LC is rotated by -45deg instead of +45deg.

R&D (FilterCavity)
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MarcEisenmann - 11:50, Friday 14 July 2023 (3289)Get code to link to this report
recovery of IRMC automatic lock

Marc, Pierre (remote)

Since the replacement of the EOM, we had difficulties to achieve automatic lock of IRMC.

This is mainly due to the fact that we're using 78MHz sidebands instead of 88MHz and had to change the PD in reflection of the IRMC for a non-resonant one.

First, the reflection signal of a scan of IRMC is different than before.

The base is at 1.38V and the TEM00 dip at 692mW while in the past the dip was negative.

This meant that we had to modify the pin P4 strap from pin 2-3 to pin 1-2.

Also, the threshold value was tweaked looking at this signal.

Then, the error signal was about 83mVpk while it was about 10 times more in the past.

Despite putting the servo gain to max I could not achieve lock (even though it was detected from the blinking LED).

I used the CCFC amplifier (32dB) and got an error signal about 2.2Vpk.

As the error signal slope and triangle scan slope are identical, the lock can be achieved with the switch INV.

I put a gain of 0.5 and could lock reliably the IRMC.